Sophia’s Status Report for 12/4

For the last two weeks, I worked on making some more repairs to the glove and adding touch sensors. The ring finger on the glove was not responding so I switched it out with a new one and stitched it down very tightly. I borrowed a sewing kit from IdEATE and sewed down it down with the full thickness embroidery thread.

I also created a new protoboard to make room for pins for touch sensors.

For touch sensors, I decided to use some conductive tape.

Unfortunately, it seems there are issues with the newprotoboard and some more of the flex sensors are not working. I will need to replace the thumb and fourth finger flex sensors next and debug my work on the protoboard.

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